April 2021
T oday’s vehicle case study is a 2011 Vauxhall Insignia which came to us because of a loss of power. It had been looked at twice by another garage to no avail. As with every diagnostic job, we started by questioning the customer so we can gain as much background information as possible. After this initial phone call, I was confident of the type of fault being presented. This was confirmed at the subsequent diagnostic assessment. On running the global fault scan, we found multiple faults relating to the turbo system with ‘underboost’ and ‘overboost’ codes alongside DPF soot accumulation codes logged in the memory of the ECU. 32 AFTERMARKET APRIL 2021 TECHNICAL www.aftermarketonline.net THIRD TIME LUCKY DPF Doctor, Chay Blyth shares his experiences with a car he was presented with after two previous fixes elsewhere had failed BY Chay Blyth, Director, Fife Autotech We followed our industry-leading DPF assessment, learned through the DPF Doctor Network practical training programme. Firstly, using smoke testing we found the split intercooler hose (see Fig.1) which coincided with our P0299 turbo underboost code. However, the assessment does not finish when we find a fault. We see it through to the end. Further testing revealed that the vacuum control solenoid was not controlling the vacuum to move the turbo actuator which then mates up with the turbo overboost code stored. Using the serial data, we could see there was also EGR and air flow issues caused by running the engine with a boost leak. Excessive soot and black smoke from the engine had choked the intake system and EGR valve. To tackle this mass of build-up soot and carbon we used the JLM Intake Extreme Cleaning Toolkit to break down the carbon. We removed the intake pipe and could see the thick ‘black death’ in the intake manifold (see Fig.2). As the chemical worked its way through, we could see on the serial data that air flow and DPF pressures were coming down. An endoscope was sent down the intake where we could see first-hand how well the intake clean had worked. We were impressed! This removed the turbo lag and flat spot at lower RPM. Rectification We went on to rectify the remaining faults. We added a Fig. 3
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